1The Disaster:
Background to the Incident:
$560 Million USD platform for the Deepwater Oil Rig was built by Hyundai Heavy Industries. The rig was owned by Transocean, under the lease of BP until September 2013. It became operational on 2010, operating at a depth of 5,000 feet. The rig acted as an exploratory well, for the construction of a well 18,360 feet deep. The plan was plug and suspend the well as a subsea producer, after the construction and cementing was complete. The well was due to be tested for its integrity and a cement plug to be set which will allow the well to be temporarily abandoned [3].
Risk assessment reports from 2009 showed that the risks of a surface or subsurface oil spillage was an unlikely event, and the close proximity of the oil rig from the shore would further prevent any severe incidents in the unlikely case any accident occurred on the rig. The oil rig was also exempted from a detailed review of the environmental impact as it was estimated that the risks for oil spillage was an unlikely event, and a blowout plan was not required from BP. The Blowout preventer that was installed on the well head has remote trigger system which can be used in cases of emergencies when the platform had to be evacuated. The rig also had a ‘dead man’s switch’ that could cut the pipe as well as seal the well automatically if the platform lost communication. However this switch was not used in the accident. IN 2003, it was however determined that the well would not need a blowout protector BOP), since all well had other backup systems to cut the well off, and additionally, the BOP could increase the costs of the well [4].
Events leading up to the disaster:
On March 2010, there were some problems faced by the rig crew while drilling mud that fell into the undersea oil reserves and sudden release of gases, as well as pipe falling into the well and the leaking of blowout preventer fluid. High pressure by the trapped gases also caused other challenges to the rig crew, however surveys before the disaster showed that BP was more focused on the drilling process instead of the safety, and that the workers often had to work with poor equipments, and were concerned about the safety practices in the organization. Even fictitious information was fed into the system by the workers, in order to avoid scrutiny, and many others afraid to raise a concern, fearing retribution. By April 2010, memo drafted by the BP warned that the casting might result in a failure, and the findings showed several signs of warning before the blowout occurred [1]. Readings from the equipments showed that there were indications of the gas bubbling into the well, which could have been the signal of a massive blowout. The gases were initially trapped by the drilling mud inside the pipe. Investigations by the Energy and Commerce Committee showed that BP adopted riskier procedures, in order to save expenses and time and even went against the advice of the contractors and internal employees. This might have resulted in increases risks of the blowout in the rig [5].
In April 2010, a fire started onboard Deepwater Horizon, and 126 crew members were onboard, which included 7 BP employees and 79 Transocean employees. Immediately following the fire, rig experienced 2 strong vibrations [1]. This was because of an abnormal pressure that built up within the marine riser as a result of which it rapidly expanded and caught fire. This buildup of pressure was due the methane gas that bubbled into the well and moved up the drilling column, expanding rapidly as it burst through many barriers and seals before it exploded. The fire engulfed the entire platform and on April 22nd, the Deepwater Horizon sank. Report published by the BP on September 8th suggested that the gases were ignited as they entered the air intakes of the diesel generators which caused a fire that engulfed the deck of the oil rig [5; 6].
The Damage:
During the time of the explosion, there were 126 peop0le onboard. This included 79 Transocean employees, 7 BP employees and 40 Contractual employees. Evacuation was possible for 115 people, with 94 being evacuated by lifeboats to the nearest supply boats, 4 to other vessels and 17 evacuated by helicopters. However 9 crew members on the platform and two engineers could not be rescued, and were presumed to be too close to the blast to escape it. By April 22nd it was discovered that massive oil spillage was occurring at the rig, at the rate of about 8,000 barrels (or 1,300,000 liters) every day [7; 8].
Reports from Investigation:
Reports from the House Committee on Energy and Commerce showed that the cement should have been tested in the well, which would have costed BP an additional $128,000 and would have taken not more than 12 hours to conduct. Reports by BP on September 2010 also pointed out that the results from the pressure tests were not properly interpreted by either BP or Transocean, and the ominous signs (like a loss of fluids from the riser pipe) of an impending disaster were ignored by both the organizations. The BP report also highlighted that even though more centralizers were not used according to the recommendations by Halliburton, it was not the cause of the disaster, and the Deepwater crew should have redirected the flow of the flammable gases to avoid the disaster, while reports from Transocean blamed the improper well design by BP for the disaster [1; 9]. On November 2010, report by the Oil Spill Commission highlighted that some decisions taken by BP actually increased the risks of the disaster, even though BP never jeopardized the safety of the workers to save money. The report pointed out that the management was trying to rush the completion, and safety culture was not very developed on the rig. A significant question was also raised by the management refuting the findings from advanced softwares on modeling that showed the need for centralizers in the rig, and the simulations were not re run to properly analyze the readings and predict the disaster [10]. The various reports on the disaster showed 6 major errors in the operation, equipments or testing in the last 32 hours before the disaster occurred. These include:
How the accident could have been avoided:
The Deepwater Horizon accident could have been avoided by developing a high level of competency in the process of deep water drilling to explore and exploit reserves situated under thousands of feet of water at the deepest recesses of earth. However, BP did not possess enough expertise in this domain, which was a significant reason for the disaster. The senior executive team at BP had the responsibility for the execution of the important actions identified as priority areas as a part of the strategic action plan to become the top company in deep water drilling. The management failed in this aspect quite significantly [16]. This could have been avoided by ensuring that ass the aspects of deep water drilling were thoroughly studied and understood, and by ensuring the highest standards of safety on the rig.
The early warning signs also should have been analyzed more thoroughly to identify the risks. Instead of neglecting the warnings and trying to save expense of the extra precautionary measures, the company should have implemented a safer practice, which could have helped to avoid the accident in the first place. The cement used for the plug should have been tested before using, which could have helped to identify its reduced density due to trapped gases. Also, the reports from the pressure tests should have been properly analyzed and warning signs such as fluid loss from the riser pipes should have been properly investigated. Recommendations from the Halliburton also should have been followed by adding extra centralizers. Similarly, using quality modeling softwares to test the reading could have also helped to predict the disaster.
According to reports, the policies by BP to reduce costs greatly increased the risks of the disaster. The organization was blamed for complacency, and most of the managerial decisions were made to avoid extra costs, and save time and money. This resulted in avoiding additional rests and modeling trial scenarios. This could have been avoided, had the company focused more on safety first and practicing the safest practices and world class safety standards in the operation of the rig [17].
Using valve technology could have also helped to avoid the disaster. According to Schilling, (2015), Automated Valves (such as the Paladin Automated Valves, manufactured by Bi-Torq Valve Automation) are controlled via an actuator that which can turn it on or off with the help of a programmable logic circuit (PLC). This control system can make autonomous decisions based upon the environmental variables which it constantly monitors (like temperature). This valve can be used in pipes that transport chemicals or fuel or even fire suppressants. The valve can be automatically opened, closed or opened halfway, and also has an override option for emergencies [18].
Conclusion:
The Deepwater Horizon shows how erroneous management practices can pave the way to erroneous decisions and operating protocols, which can endanger the lives and well being of the employees, especially in high risk workplaces such as oil rigs. It is vital therefore that the organization adopts the best international safety practices to avoid such disasters, and employ advanced technologies for testing the operation thoroughly before implementing it. Following the safest work standards it can be possible that such oversights are avoided and the best working practice is used.
Engineering is the science and technology that is used to meet the demands and needs of the society, which includes construction of buildings, bridges, tunnels, vessels or aircrafts, and developing newer technologies and infrastructure. To meet such needs, the engineers and the managers often needs to devise a mutual strategy to address the demands, and can lead to shortcuts be taken in this process, in order to cut costs or margins. These shortcuts also increase the risks of errors and thus engineering failures and disasters that are caused due to design failures. Such can even cause massive loss of property as well as lives. Different engineering failures have occurred within our modern history. The deepwater Horizon explosion was a significant engineering accident that occurred in 2010 that resulted in the sinking of the Deepwater Horizon oil drilling rig, the death of 11 workers, injury of 17 others and a massive oil spill into the Gulf of Mexico, that lead to an unimaginable environmental impact, due to which it was considered the largest environmental disaster in the US history
References:
[1] BP (Firm). Deepwater horizon accident investigation report. BP, 2010.
[2] Bly, Mark, ed. Deepwater Horizon accident investigation report. Diane Publishing, 2011.
[3] Svanberg, Reinert. “Integrated Operations in light of the Deepwater Horizon accident.” Master’s thesis, Norges teknisk-naturvitenskapelige universitet, Fakultet for ingeniørvitenskap og teknologi, Institutt for marin teknikk, 2011.
[4] Skogdalen, Jon Espen, and Jan Erik Vinnem. “Quantitative risk analysis of oil and gas drilling, using Deepwater Horizon as case study.” Reliability Engineering & System Safety 100 (2012): 58-66.
[5] Dadashzadeh, Mohammad, Rouzbeh Abbassi, Faisal Khan, and Kelly Hawboldt. “Explosion modeling and analysis of BP Deepwater Horizon accident.” Safety science 57 (2013): 150-160.
[6] McNutt, Marcia K., Rich Camilli, Timothy J. Crone, George D. Guthrie, Paul A. Hsieh, Thomas B. Ryerson, Omer Savas, and Frank Shaffer. “Review of flow rate estimates of the Deepwater Horizon oil spill.” Proceedings of the National Academy of Sciences 109, no. 50 (2012): 20260-20267.
[7] Skogdalen, Jon Espen, Jahon Khorsandi, and Jan Erik Vinnem. “Evacuation, escape, and rescue experiences from offshore accidents including the Deepwater Horizon.” Journal of loss prevention in the process industries 25, no. 1 (2012): 148-158.
[8] Ramseur, Jonathan L., and Curry L. Hagerty. “Deepwater Horizon oil spill: Recent activities and ongoing developments.” Congressional Research Service. January 31 (2013): 2013.
[9] Cleveland, Cutler, C. Michael Hogan, and Peter Saundry. “Deepwater Horizon oil spill.” The encyclopedia of earth(2010).
[10] Skogdalen, Jon Espen, and Jan Erik Vinnem. “Quantitative risk analysis of oil and gas drilling, using Deepwater Horizon as case study.” Reliability Engineering & System Safety 100 (2012): 58-66.
[11] Segura Trull, Sergi. “Deepwater horizon: Explosion, fire and sinking. Research and, analysis of the causes, consequences and proposals for improvement.” (2012).
[12] McNutt, Marcia K., Rich Camilli, Timothy J. Crone, George D. Guthrie, Paul A. Hsieh, Thomas B. Ryerson, Omer Savas, and Frank Shaffer. “Review of flow rate estimates of the Deepwater Horizon oil spill.” Proceedings of the National Academy of Sciences 109, no. 50 (2012): 20260-20267.
[13] Kujawinski, Elizabeth B., Melissa C. Kido Soule, David L. Valentine, Angela K. Boysen, Krista Longnecker, and Molly C. Redmond. “Fate of dispersants associated with the Deepwater Horizon oil spill.” Environmental science & technology 45, no. 4 (2011): 1298-1306.
[14] Bly, Mark, ed. Deepwater Horizon accident investigation report. Diane Publishing, 2011.
[15] Park, Jeryang, Thomas P. Seager, and P. Suresh C. Rao. “Lessons in risk?versus resilience?based design and management.” Integrated Environmental Assessment and Management 7, no. 3 (2011): 396-399.
[16] M. Watkins, “How BP Could Have Avoided Disaster”, Harvard Business Review, 2010. [Online]. Available: https://hbr.org/2010/06/global-strategy-local-policies. [Accessed: 29- May- 2018].
[17] S. Goldenberg, “BP cost-cutting blamed for ‘avoidable’ Deepwater Horizon oil spill”, the Guardian, 2011. [Online]. Available: https://www.theguardian.com/environment/2011/jan/06/bp-oil-spill-deepwater-horizon. [Accessed: 29- May- 2018].
[18] D. Schilling, “Valve Technology Could Have Prevented Deepwater Horizon Explosion – Industry Tap”, Industry Tap, 2015. [Online]. Available: https://www.industrytap.com/valve-technology-prevented-deepwater-horizon-explosion/15062. [Accessed: 29- May- 2018].
Essay Writing Service Features
Our Experience
No matter how complex your assignment is, we can find the right professional for your specific task. Contact Essay is an essay writing company that hires only the smartest minds to help you with your projects. Our expertise allows us to provide students with high-quality academic writing, editing & proofreading services.Free Features
Free revision policy
$10Free bibliography & reference
$8Free title page
$8Free formatting
$8How Our Essay Writing Service Works
First, you will need to complete an order form. It's not difficult but, in case there is anything you find not to be clear, you may always call us so that we can guide you through it. On the order form, you will need to include some basic information concerning your order: subject, topic, number of pages, etc. We also encourage our clients to upload any relevant information or sources that will help.
Complete the order formOnce we have all the information and instructions that we need, we select the most suitable writer for your assignment. While everything seems to be clear, the writer, who has complete knowledge of the subject, may need clarification from you. It is at that point that you would receive a call or email from us.
Writer’s assignmentAs soon as the writer has finished, it will be delivered both to the website and to your email address so that you will not miss it. If your deadline is close at hand, we will place a call to you to make sure that you receive the paper on time.
Completing the order and download